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Previous modifications (that I know of):
- AVO pod filter
- GFB crank pulley
- Aftermarket secondary CAT (might be hi-flow)
- EcuTek tune
- White line front and rear sway bars
- Brandt disabled or removed
- Aftermarket alarm system
Ordered the O2 sensor through one of my father's supplier only to be sent the rear one instead of the front. Got quoted a crazy price for the front A/F sensor so I went online... Plugged it in and all was good. Little did I know I had just created the biggest headache for myself later.
Initially I thought I got a good buy but with limited knowledge about twin turbos I didn't pick up that it had a low boosting primary too. I soon discovered I really had a problem when I occasionally tripped a turbo related code up steep hills. This code put the car in limp mode. The car would be struggling in the primary rev range but suddenly burst to life when the secondary engaged, only to be thrown forward in my seat due to the limp mode boost cut.
The McIntosh sound system had seen better days. Discovered it was 8Ohms so I ripped it all out and reran new wiring and installed speakers, head unit and a sub.
Saved up my pennies and found some similar turbos online. The VF21 and VF13. Bought and installed them. These bought the car to life. I was very happy with it despite a too lean error code. However, about a month later when visiting my family and about 10kms from their place the primary turbo blew up. Ended up limping through the main street of Bellingen with a huge cloud of black smoke behind me. The day before I had noticed erratic boosting and had found the wastegate hose split! Got 6km from my destination and car was really struggling, got out and checked the oil level. Bone dry. Poured a crap load of oil into it and managed to get there. It used almost all the oil I put in it over the 6km.
Pulled the car apart. Here's what I found:
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I hoped to find most of the shrapnel in the intercooler. Alarming found nothing. It had been blown through the engine. Knowing full well the engine could be stuffed, I rebuilt my original primary turbo using a kit I got online anyway. Discovered the primary had be seized due to oil leaking into the exhaust side and being baked on. Took to it with a wire buff. Threw the new bearings from the kit in and put it together. I didn't have the tools to balance it and knew it may not last, but 20,000kms or so later it is still working.
After this the car ran great apart from using a lot of fuel and throwing a too lean code. Replaced a number of parts in vain. That's when I joined SubyClub. Flogged the life out of that thread for a long time. Added a silicone intake pipe, phenolic spacers and new vacuum lines. Fixed air leaks, smoke tested it and ran diagnostics. Replaced the BBoD, MAF, CTS, intake manifold and much more. It was a hell of a journey and spent more money than I'd like to admit only to find out it was the knock off O2 sensors I had bought. Thanks again to all who helped.
During this troubleshooting sega I needed a new clutch. Ended up replacing the box to sort out the previously mentioned whine. It had got louder over time and sourcing the bearings would be expensive and difficult. Bought a HD clutch. In total cost me $1500. A bit disappointing that the new box has a few troublesome syncros, but still better condition than the old box.
I buggered up my rear passenger door when I scraped past a tap at my old place. It was in the most inconvenient spot. A friend ran it over the very next day. We plugged the hole so there would be no more victims. I also happened to reverse into an old Navara and stuff up my rear bumper. Got a new door and bumper from Kong. Door is on but I'm going to sand and spray the bumper. Also got keyed...
Had several flats over a short period of time. Ended up over-using the temp wheel and blowing it up too. Bought a whole set of BBS rims in good nick with new tires for $450. Ditched the temp and have a real wheel in the back plus 3 other spares at home. The last set of front tires got rotten inner edge wear so I got an alignment.
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I've done a few other things like sway bar bushes, battery, coil packs, plugs and replaced a fog light.
Anyway, this car has been a huge learning experience. A fair bit more complicated than the Magnas I had before. Up to 199,000KM now and the engine has survived being starved of oil, fed metal shavings from a blown turbo, messed up A/F rations and of course the odd flogging.
I still have a few things to fix...
Engine/clutch shudder:
Doubt it is the clutch. The fly was machined and spigot replaced, etc. Suspect it is engine mounts.
Cam shaft sensor:
Rough start up and idle, especially with the lights on. Suspect a bad earth or alternator problem.
Lastly, I'd like to build a box around the pod filter to help shield it from drawing in hot engine air.
I'll update this thread if I have forgotten anything or have new stuff to add.