Had a few problems that have been ignored/worked around while sorting out the whole leaky valves situation but now the valves are working well and the primary is boosting as it should it was time to address these issues. First issue was that it would not run well with rich AFR's and boost so as a work around I just had the afr's set at low 13's while under boost. This gave the engine very little power but that was of no concern as the issue was getting the valves to function correctly and allow the primary to boost. With the valves sorted it was time to add some fuel and increase the power but over 4000rpm and approaching 1 bar boost, increasing fuel was causing horrid misfires on all plugs, pulling the plugs showed they were extremely fouled from carbon. The plugs that were fitted were just basic Bosch plugs so as a test these were removed and a set of used iridium plugs were fitted to see if there was an improvement. There was not:
The shiny specks on the end of the electrode look like bits of metal and at first I thought it may be bits of piston but surely I would of heard detonation if it was that bad? Turns out it was just clear specks on the electrode so I don't think it was anything nasty, it was possibly just starting to burn off by the time I got the car back to the garage to pull the plugs.
I moved ignition timing up and down by quite a degree to double check that it wasn't a timing or knock issue causing the poor spark but the result was the same regardless of timing so next was to try and crank up the dwell. I had this setup at 3ms but I don't have a scope to test the coils to see if that was accurate, I blindly set it to this based on an article I found online for these coils that was released by 'Link'. So as a test dwell was increased to 5ms, again I can't check with ascope whether this is too much but the coils weren't getting hot so I took it for a drive and the misfiring definitely improved. It was still breaking down but AFR was richer and was now in the mid-high 12's. Pulling the plugs again they were still caked in soot and being used (well used actually) they were probably at the end of their life so I threw in a new set of basic NGK's (BR6E) and the problem was then solved. No more misfiring and was happy to run AFR's of 10's and 11's. I keep forgetting to turn the dwell back down to double check whether the dwell was the culprit or whether it was simply bad plugs as I am curious since the bosch plugs were not very old at all. I guess they could have been killed while the tune was a bit rough though.
Next problem was one that I also have known about for a while but just didn't bother with it as it was out of the way at the time. It is a sync issue at 6500rpm. With the valves working, no more misfiring, a smoother changeover and the engine making a bit more power it was time to push the engine to the red line and ensure that there is perfect sync so that I can finally get this on the dyno and try and get some power out of it.
I think it was talked about on previous pages but just to refresh, basically the biggest issue with this ecu is getting a clean signal from the VR sensors for the cam and crank. The sensors on these apparently throw out a very large voltage at higher rpm and a low voltage at lower rpm/cranking speeds making it further difficult to set the correct trigger levels. There is also a lot of noise in the signal that gives a lot of false triggers. To try and cut it short, the standard circuit's could not tolerate the noise from the sensors and it was impossible to even get the engine to start. Through trial and error the noise from the crank sensor was cleaned up using an inline resistor and the noise from the cam sensor was cleaned up using an inline resistor in combination with a shunt resistor to ground. The trigger levels for both were set as high as they could be before blocking the signal's entirely at crank speeds. With the noise removed the ecu could happily sync with the engine position however another problem turned up as the rpm begin to increase and it was again losing sync. By looking at the trigger logs I eventually worked out that one of the teeth on the cam wheel was being filtered out at higher rpm (if I recall it was ~3500rpm at that point of lost sync). By looking at the circuit schematics and with the help of google and some lucky guesswork I figured it was a capacitor that was causing the grief and again through trial and error the suspect capacitor was replaced with smaller and smaller values until full rpm could be reached. The max rpm before sync loss would increase as the cap size was reduced. At the time, with a sloppy tune and open wastegates to restrict boost, it was able to reach just shy of 8000rpm with no sync loss by reducing the value of the capacitor from 220nf to 22nf.
This is a screenshot of one of the trigger logs that show the missing tooth:
Now that engine power has stepped up a bit another sync error has popped up at 6500rpm. The tooth logger shows it as noise this time though rather than a missing tooth. To try and clear the noise I added another 10nf cap in parallel with the 22nf as the next largest cap I had on hand was a 56nf which I know from previous experiments was too large and would filter out the third tooth on the cam wheel as well. The combined 32nf of cap was too large though and also filtered out the third tooth.
This is a screenshot of the noise:
I haven't fixed this issue yet but I find it interesting in the way the ecu responds to each sync loss. With the noise at 6500rpm it acts more like a nasty misfire and if I keep the peddle mashed it will re-sync and try it's hardest to push through the error. With the missing tooth it's a horrible violent complete shutdown that needs a restart to re-sync. When I added the 10nf capacitor and took it for a run I shit bricks when the loss hit, it was just below 6000rpm, secondary was online, afr's were rich and boost was high and it just shutdown with this god awful massive explosion. The car rolled to a stop with the engine shutdown but still popping and backfiring and I thought for sure I was picking up bits of engine off the road but luckily it was all just noise and show. Everything was fine, engine restarted perfectly and I promptly drove it straight back to the garage and ripped that capacitor straight back out.
The injectors are actually maxing out at ~6000rpm at 1 bar as the afr leans right out. The duty cycle at this point is ~165% as well which means that the injectors are basically not closing at that point. With this in mind and the way the ecu behaves to the noise, I am wondering whether the cause of the noise is actually a consequence of the maxed injectors and the symptoms these will produce, such as a possible decrease in fuel pressure, certain cylinders leaning out more than others, detonation and so on.
I could try adding additional inline resistors but I doubt this will have much effect as there is already 50k of resistors wired in and although I can't remember what the resistance of the sensor is at this point I am pretty sure it is a lot less than this. I will double check this anyway.
I think I might just replace the injectors with some larger units first though since I really should have already done this anyway.