Today’s effort was a roller coaster ride early on. With this fuel pump wiring I decided overnight to just do a patch wire job and sealed each wire with some heat shrink for the time being. I found a 9-0791 install kit for the DW200 for a good price on eBay so I made a purchase, this will replace the wiring and the sock.
I discovered last night that the DW200 fuel pump comes in a kit that includes the 9-0791 install kit for the same price as the kit I purchased a number of years ago. Bit annoyed about that!
With the temporary wiring decision made, it was done and installed. I put the 20L of fresh 98 that I got yesterday into the tank and decided to flush the input line at the engine end to get rid of any last remaining dead fuel. No bueno.
Looked into it and I couldn’t get the pump to prime. I checked fuses, hot wired the pump at the tank and decided it might be my joints I just twisted together and heat shrank.
I set up a “test bed” on a cardboard box on the ground (because my shed is awesome - it was f’n hot today too!) and found that the pump was trying to turn but was seized. By this stage I was full spewing - what a waste of money etc. After pacing around I spoke with Mrs El_Freddo and told her what was going on - as I did this I shook the pump and I felt the centre of it click a little. Back to the test bed and while hitting the positive to activate the pump I shook it in the same manner and it came to life! Stoked!
Back in it went and purged the fuel line no worries. It’s also super quiet which I was really stoked about - no whining noises! Now waiting on the install kit with the proper wire and new sock in it to fit and forget about this part of the build.
With that done I got the engine to idle really roughly with my ghetto turbo bypass intake system - I borrowed Ruby Scoo’s NA EJ22 intake and plumbed in the IACV and crank vent system, plugged off what wasn’t needed and hooked up the AFM. It wouldn’t start on its own accord without the use of some starter fluid like yesterday - but this time it kept running, albeit quite roughly. But it ran with its own fuel system. STOKED!
I’ve got an exhaust leak at the base of the up pipe, hoping it’s just a loose fitting or a new gasket required. It could be a split up pipe from what I’m told - I’m learning quite a few bits about these machines which is awesome!
At this point I need to make a shout out to RSguy (Rob Z) from the RSLC forum who was very helpful with my questions and requests over the last few days! He’s the only person I know/have contact with that also owns and knows RSs.
I rigged up the cooling system that bypassed the heater core because I didn’t want to hook it up due the PO who put a T piece in one of the lines (driver’s side) with a smaller diameter off shoot that I can’t work out what it’s for. I still don’t have a coolant temp sensor hooked up - I need to source a plug and I’m reluctant to cut one off another loom in the shed that might be used in the future. I’ll get one sorted at some stage. This could be the hard starting issue I’m experiencing.
With the cooling system hooked up I could give it a longer run and found another vacuum leak to deal with. I made a super ghetto IAVC pipe setup with a small section of rad hose, another piece of the factory IACV plumbing and some duct tape! It still stumbles around a bit when idling - not like it’s sorting out it’s idle on first start with the battery reconnected.

Interestingly, even with the 40° weather today, there was still exhaust vapour that could be seen. It didn’t smell odd, but I am running tap water too - this is because I’ll open up the cooling system again soon, I also didn’t want to waste good coolant if there was a big issue to deal with. Hoping this vapour just exhaust vapour/crap from sitting so long and not anything sinister! No bubbles in the remote res so that’s a positive.
And that was play time over. I made it to the goal I wanted to achieve, mind you a few things were different to the original plan (namely the turbo bypass intake setup) and it was two days later than i thought. Can’t complain, I essentially had two days off from the project last week and I still made it before the end of my holidays so it’s a win! Plus my eldest got in on the action for a few days before the stupid hot weather kicked in.
Now it’s dawned on me - I’m into that “10% that takes 90%” zone with the engine bay etc. What needs to be done now:
- clutch hydraulic system overhaul (then it’ll move under its own power!)
- engine mount nuts.
- inspect the up pipe/fix exhaust leak from this area.
- dump pipe gasket fitted (no gasket atm for test purposes) along with all required nuts and bolts.
- buy new turbo elbow - my one is proper rooted with a super dodgy repair!
- pitch stopper rod bolted in.
- charcoal canister mounted and its third line to/from it sorted. I need to work out where this goes/comes from.
- sort out the temp sensor plug and wiring, locate the engine wiring loom under the back of the intake manifold where I think it’s meant to be - intake manifold will need to be lifted for this (fun!)
- sort out turbo intake tract pieces and find the missing bits I apparently don’t have - removed for a catch can by the PO I think.
- source a new brake master cylinder cap - noticed mine sports a split in the centre of it. Not ideal!
- bolt in the auxiliaries and fit the fan belts
- fit the thermo fans
I’m sure there’s more in there - that’s a general run down!
Things will no doubt slow down a bit with this one now. I’m hoping to keep pushing along with it when I can.
Thanks for reading for those that took the time to do so. And another shout out for all the help from Rob Z/RSguy!
Cheers
Bennie